An Emergency Request For A Steam Trap Testing Audit
Challenge:
Customer complained of high back pressure in their condensate system. He believed that the problem was failed steam traps.
Solution:
Bruce tested the 250 steam traps and found a failure rate of 23 percent. Around each steam trap was a bypass VALVES. Failed steam traps did indeed have a direct bearing on the problem he was called into solve: Abnormally High Back Pressure in the Condensate System. However, there was another contributor to the problem. After ultrasonically testing the bypass VALVES around steam traps, he discovered a ?" bypass valve had inadvertently been left open by a contractor that had replace a steam trap. Because it was a low rise valve it was not easily identified. The sound emitted from the totally open valve in this 150 psi steam system was huge. He heard the open valve a good distance away before he approached the problem area. The HVAC mechanic proceeded to close the valve that had no business being left open..
Results:
Problems solved. Bad steam traps were replaced within a week of their identification. Locking caps were placed on each bypass valve--this would prevent the same contractor or any unauthorized personnel from opening one in the future.
The open 3/4" bypass valve @ 150 psi steam pressure (24 hrs per day and 365 days/yr.) and a steam cost of 10.50 per/1,000 lbs. of steam produced represents a loss of approx. $207,000.00. The additional traps found leaking and blowing at the facility amounted to a loss of $ 67,000.00. The total approx. loss at the facility was $274,000.00.
Yearly audits are now scheduled and the company claims they have hundreds of thousands of dollars in annualized savings from proper trap testing and leak identification.